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HomeMy WebLinkAbout2004 02 13 - Flow in Blossom DitchLIM t 2301 Maitland Center Parkway, Suite 300 Maitland, Florida 32751 tel: 407 660-2552 fax: 407 875-1161 February 13, 2004 Mr. Ken Jones City of Sebastian Stormwater Department 1225 Main Street Sebastian, Florida 32958 Subject: Flow in Blossom Ditch Dear Mr. Jones: Per your request CDM has reviewed the ICPR model utilized in the Sebastian Master Stormwater Management Plan to obtain representative flows in the Blossom Ditch for the Mean Annual, 25 Year and 100 Year design storms (all of 24 hour duration). This information was for comparison with Masteller and Moler, Inc. (M&M) flow estimates documented in a letter dated September 3, 1998. As was noted in the City's Stormwater Master Plan, one of the identified capital improvement projects was to provide a cross drain under Roseland Road to link the Wentworth Ditch to the Blossom Ditch, as such two sets of flows will be reported. The first will be the flow in Blossom Ditch solely as a result of runoff within Unit 5; the second will include the additional flow based upon the modeled improvement. These flows are compared with the flows reported by M&M in the table below. Storm Event M&M Flow (cfs) CDM Flow — Unit 5 (cfs) CDM Flow — Unit 5 and Cross Drain (cfs) Mean Annual 34.6 61 85 25 Year 84.02 88 104 100 Year 113.67 94 110 As M&M's model schematic was not included in the cited letter, the assumption was made that the locations were comparable. In the case of the CDM ICPR model, the flow was taken from conduit ID "P-node9" which is the representation of 54" RCP M&M proposed and was included in the model. The configuration of this conduit was based upon plans obtained from City staff, dated December 1999 and revised May 2000. 8:@058Z3305AConLlr 04Feo13.doc consulting - engineering - construction • operations Mr. Ken Jones February 13, 2004 Page 2 As noted in M&M letter, it was stated "the diversion system should be designed for the 100 - Year Storm Event." If one refers to the above table, it is noted that the flows reported by M&M are approximately consistent with CDM's estimate (113.67 cfs compared with 110 cfs). The proposed pipe size (54" RCP) appears appropriate to convey the 100 -Year storm event. If you have any questions please call either myself ((407) 660-6315) or Eric Grotke ((772) 231- 4301). Ve/ly your D las?. P.E. Project Engineer Camp Dresser & McKee Inc. cc: Dave Fisher Eric Grotke SA20582V305MCor1U, Web13doc